Suzhou Electric Appliance Research Institute
期刊號: CN32-1800/TM| ISSN1007-3175

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一起超高壓變電站低抗絕緣油檢測異常缺陷分析

來源:電工電氣發(fā)布時間:2023-03-04 10:04 瀏覽次數(shù):369

一起超高壓變電站低抗絕緣油檢測異常缺陷分析

王從剛,錢苗旺,郁飛
(國網(wǎng)江蘇省電力有限公司連云港供電分公司,江蘇 連云港 222000)
 
    摘 要:針對一起在超高壓變電站油浸式低壓并聯(lián)電抗器 (低抗) 絕緣油檢測中發(fā)現(xiàn)總烴超標的事故,通過對絕緣油溶解氣體含量分析,借助三比值法初步推斷低抗內部存在中溫過熱故障,進行包含直流電阻、絕緣電阻、阻抗、介損及電容量等項目的診斷性試驗,分析低抗缺陷原因,并對低抗進行解體驗證。結果表明,低抗缺陷的原因為接地屏中存在銅箔片異常搭接,進而引起環(huán)流引發(fā)局部過熱,造成異常搭接處被灼燒,導致總烴超標。
    關鍵詞: 變電站;油浸式低壓并聯(lián)電抗器;總烴;過熱故障;缺陷分析
    中圖分類號:TM472 ;TM855     文獻標識碼:B     文章編號:1007-3175(2023)02-0047-04
 
Analysis on Abnormal Detection of Low-Voltage Parallel Reactor
Insulating Oil of a Ultra-High Voltage Substation
 
WANG Cong-gang, QIAN Miao-wang, YU Fei
(Lianyungang Power Supply Branch, State Grid Jiangsu Electric Power Co., Ltd, Lianyungang 222000, China)
 
    Abstract: An accident which the total hydrocarbon from insulating oil of the oil-immersed low-voltage parallel reactor of a ultra-high voltage substation exceeded standard happened, so the paper analyzes the dissolved gas content of insulating oil, and it is preliminarily inferred through three-ratio method that medium temperature overheat fault exists inside of the low-voltage parallel reactor. Then, diagnostic tests are conducted on DC resistance, insulation resistance, impedance, medium loss, and capacitance to analyze why the low-voltage parallel reactor has defects, and disassembling the low-voltage parallel reactor verifies the correctness of this analysis. According to the results, the reason for defects of the low-voltage parallel reactor is that copper foils in the earthing panel are connected abnormally. As a consequence, circulating current contributes to local overheating and the abnormal connection burns, causing the total hydrocarbon exceeding standard.
    Key words: substation; oil-immersed low-voltage parallel reactor; total hydrocarbon; overheat fault; defect analysis
 
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